DeLONGH1 ECM550.75 PRIMADONNA CLASS Repair
|
 |
|
Above is a picture of
the coffee machine as it was when brand new ... not actually
the example I'm repairing but let me describe its problem. It
faultlessly makes a jolly good cup of coffee, but if the steam
feature is used, the thing trips the mains supply. A bit annoying
so I suggested that I fix it.
Getting it apart is straightforward
if you have a Torx T20 bit with a security hole down the middle
plus a Philips T1 screwdriver and sufficient confidence in unclipping
exceedingly stiff plastic brackets.
First remove the rear cover
then the two side panels to see a mish-mash of parts, wiring
and plastic tubes. At the left side (looking from the front)
you can see the steam producer carried under that perforated
black plastic cover.
|
|
 |
|
The cause of the tripping
was already pretty well established and is fairly common... being
associated with a water leak at the boiler assembly used for
producing steam. Sure enough there was lots of corrosion and
traces of limescale or otherwise calcium carbonate at the end
of the boiler tubes. Removing the boiler assembly looked complicated
but turned out to be fairly straightforward. A set of very tight
plastic clips hold in place the lid of the boiler assembly. There
are also two pairs of push-on mains clips which need to be removed.
Once I'd moved the assembly clear of its position I also found
two ground wires. These have ring terminals secured to threaded
parts of the mains tags (to which the pairs of clips are connected)
by 7mm nuts. By carefully pulling tubes and wiring away from
the boiler it can be detached.. or almost detached... because
this model of machine has a temperature sensor clipped onto the
boiler. This wasn't easy to detach in situ due to limescale so
to free this means getting access to the controller circuit board,
locating the two pin temperature sensor plug and pulling this
off. It can then be jiggled free from assorted clips and tie-wraps
so the boiler can be removed. The temperature sensor can then
be detached (it was completely coated in limescale) |
|
|
|
|
Once the boiler assembly
has been detached the spring clip can be levered away from its
mounting position allowing the temperature sensor to be pulled
away from the boiler tubes. Here you can see lots of corrosion
and this probably affects the operation of the sensor slightly,..
allowing the temperature to rise higher than planned due to poor
adherence to the metal.
Once the sensor has been detached
the boiler tubes can be separated from its plastic cover, but
due to the corrosion I decided to initially unplug the far end
of the sensor cable.
|
 |
|
 |
The sensor cable comprises
two pretty thin leads about 3 feet in length and threads its
way to the control circuit board mounted on the opposite side
of the coffee maker.
The sensor plug connection is
at the bottom left corner of the control board as seen below
and can be readily pulled off.
|
|
 |
 |
 |
|
These pictures show the
clean state of the end furthest from the leak, the heavy corrosion
at the leaky end and a view inside the end of one of the pair
of boiler tubes which clearly shows a partial blockage from chalk
build up.
At this point I guessed the
boiler assembly just needed cleaning.
|
 |
|
I detached the plastic
covers at the ends of the assembly and pulled out the plastic
input and output tubes. One was nice and shiny but the top one
showed some tarnishing and limescale which allowed steam or water
to escape under pressure.
The picture was taken after
treating the collar with brass brush held in a high speed drill.
I then carried out some electrical
leakage tests which proved puzzling.
|
|
 |
|
|
First of all I measured
the resistance between the mains wires and the metal body. Bearing
in mind the residue present at one end of the boiler is bone
dry I didn't expect to see much leakage. In fact the leakage
varied quite a bit between about 7 and 14Mohm, using a standard
multimeter but, if a water was present when the steam feature
was turned on, the leakage would be a lot lower ( measured about
2Mohm when the terminals were damp). However as I made measurements
something seemed wrong as the resistance between the metal casing
and the mains wires sometimes dropped to 1Mohm so I immersed
each end in white vinegar to dissolve the chalk residue. This
worked fine but the leak was still present so I decided to test
the thing using a high voltage power supply instead of my low
voltage multimeter. See pictures below.
Much to my surprise, connecting
400 volts between the casing and one of the element mains connections
drew 500mA. I reduced the supply voltage and eventually the leak
reduced intermittently somewhat to about 25mA. Clearly there's
a problem. I found that the pair of elements both ran hot with
HT plus at one of the mains wires and HT minus at the casing
so this leak is surely what was tripping the mains supply. My
guess is that the tubes carrying the heating elements are not
hermetically sealed and water ingress has resulted in shorts
inside the tubes. Looking into the end that wasn't at the leaky
plastic tube it appears that this indeed is not sealed so water
probably penetrated the end at the water leak causing corrosion
which bridged the elements and the metal casing.
The next morning I checked the
leakage with my multimeter again and got a very puzzling result.
One end shows 11Mohm to case and the other was 3Mohm to case
with the element reading 44 ohms (ie. two 88 ohm elements in
parallel) which I initially couldn't explain, but after a few
moments I realized that what I'm seeing is diode action from
limescale and sure enough reversing the multimeter leads reversed
the readings.
I've ordered a new heater assembly.
|
 |
|
|
Summarising... The coffee
machine has been run from particularly hard water during its
life. This has resulted in deposits of limescale within the steam
boiler assembly, especially around the plastic end caps. This
has had two effects. Firstly the limescale deposits resulted
in increased water pressure which strained the leakproofness
of the joints. Secondly the deposits infiltrated the joints.
The input and output joints each use a tapered brass bush which
at the ouput end has reacted to the chalk and steam resulting
in heavy tarnishing which compromised the joint seal. Steam was
then allowed past the seal and settled on the area carrying the
electrical connections. Additionally steam or water penetrated
the end seals and ruined the insulation between the heater elements
and the surrounding metalwork once the electrical leakage was
high enough it was detected by mains leakage detector which tripped.
During this process the temperature sensor element lost its adherence
to the boiler assembly resulting in poor temperature regulation
probably speeding up the failure of the boiler assembly. |
|
|
First, left is the new
boiler assembly whose measurement shows perfect isolation between
the mains connections and the casing.
Then, below is the old boiler
assembly showing the the pair of readings which are indicative
of diode action. I then applied 400 volts across the mains wiring
and the case and saw the HT supply initially folding from the
initial voltage but indicating a leak of 500mA with the casing
running fairly warm. The current gradually fell but settled around
25mA with the HT voltage rising back to normal. A mains supply
would have tripped because of potential safety ground current.
I inspected the sealing (or
lack of hermetic sealing) of the mains connections of the new
boiler assembly and found that it was very likely that water
could penetrate into the winding space.
|
 |
 |
 |
|
 |
|
Two pictures showing the
fitting of the new boiler assembly. The connections from the
temperature sensor were then secured in place using tie-wraps
en-route to the controller circut board, then all the panels
were clipped back in place and secured with their fixing screws. |
|
 |
 |
|
Switching on revealed
everything seemed to be working normally although a descaling
message suggested this needed to be done. In fact the message
had appeared some time ago but as the descaling involved turning
on the steam boiler the process had never been completed because
the mains supply tripped once the boiler supply was switched
on. |
|
|
|