Hewlett Packard HP8640A
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Here's a view of my latest
HP acquisition. Not exactly as it seems because the range knob
dial is just resting on the panel and the left handle is snapped
off at the bottom. Hopefully I can sort these things out and
clean up the corrosion on the alloy fittings. At least the panel
looks clean and tidy. It remains to be seen whether the various
switches and mechanism parts are in good order. The tuning is
a little stiff but may just be lack of lubrication or a build
up of surface corrosion.
I've shown below the differences
in panel layout between A and B examples. Clearly the A version
has no built-in counter but I understand its spectral purity
is superior to that of the B version. |
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One of the first tasks
will be to find a suitable knob for the range control and to
fit back the dial then remove the panels and see how the thing
has fared over the years and make a judgement on refurbishment.
I quickly found a suitable knob for the range switch and fitted
it but the thing failed to turn and because of the complex plastic
gear train behind the panel I didn't force it to rotate until
I'd investigated further. Initially I detached the top cover
which needed lots of persuasion due to heavy oxide deposits but
it freed up to reveal a light covering of yet more oxide. An
old electric toothbrush soon removed most of this as well as
some of the lettering on the largest panel. Oddly, although the
top and bottom seals were intact, whoever had last been inside
had fitted the panel covering the innards back to front (easy
to spot because arrows should point to the power supply pcbs
at the rear of the chassis). I cleaned up everything including
the fan blades which were smothered in aluminium oxide. To complete
this area I had to detach the metal filter. Once happy with the
results I refitted a cleaned up lid and turned the chassis over
so I could detach the lower cover. This covers amongst other
things the plastic gears which I felt were probably going to
be pretty rough. |
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What's left of the range
knob removed. Now, I must signal a warning to anyone contemplating
working on an HP8640 signal generator, which is to purchase a
set of suitable Allen Keys. Many knobs are fastened with 0.05
inch grub screws and these may well be seized and can only be
removed with a good quality 0.05 inch key. |
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The rear panel shows that
this equipment indeed is fitted with Option 2, an internal doubler
extending the range to over 1GHz.
Voltage selection is accomplished
by pulling out the fuse assembly and refitting in the alternative
mains setting position.
Nice to have an IEC connector.
Below is a picture of the underside
of the top cover. |
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Above is what was revealed
under the top cover. Not too bad and amazingly you'll see the
extender board for testing pcbs and a set of spare fuses in the
plastic cup lower left (and below). Thankfully the tuning dial
cord (below left) looks intact and in perfect condition... |
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Above is the pcb under
the back-to-front lid. Apart from a trace of rust on one gold-flashed
chip the thing looks perfect and after detaching the lower lid
everything looks perfect apart from a thin coating of dust. All
the plastic gears look intact although they seem to be stuck
from dried grease. All the other gears such as those attached
to the attenuator etc also look perfect. |
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Under the air filter was
a mass of debris and aluminium oxide which readily cleaned up.. |
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Above is the view once
the lower lid had been detached.. even the spanner (centre right)
was present..
I'm really pleased to see yaxley
switches instead of the abortionate spring-clip devices used
in the HP8640B.
Now to look at the gears etc
and see if they need lubricating.
All the range gears were OK
and I added some copper-ease grease to these and the low pass
filter operating mechanism, however I spotted a couple of tuning
gears with cracked centre bushes. I could superglue these later
to preserve them. The reason for the cracking was probably due
to unequal expansion of the plastic and brass bushing. Unfortunately
the smaller centre gear of the main tuning gear has a missing
tooth. This hardly affects operation as it stands but I did find
the tuning pointer doesn't move to the extreme left. In fact
at the furthest point about an inch from the end, reversing tuning
causes the dial cord to unwind and slip from its bush. I managed
to refit this using a pair of tiny crochet hooks but this problem
is the likely reason the equipment was set aside.
Clearly the tuning needs to
be resynchronised after making good the missing tooth. The tuning
for the cavity oscillator has a saeries of disks which allow
for a pair of mechanical end stops, but if the gears connecting
to the cavity gear slip out of position I can envisage a tooth
breaking off due to excess pressure used in rotating the knob.
In fact this area was found to be faulty when I refurbished my
HP8640B.
Below are some documents which
comprise Service Sheet C in the HP8640A manual. Click to see
full size. |
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In fact. although I read
these pages I hadn't appreciated the clever design of the tuning
and wavechange display. Removing a few screws enables the entire
assembly to be merely withdrawn from the equipment. The dial
cord arrangements in their entirety are then exposed just as
shown in the pictures above. But why did I need to remove the
display assembly? Well, basically something was jamming up. A
previous knob twiddler had broken off a tooth on a gear and anyway
the pointer didn't reach the extreme left side of the dial. If
an extra turn to overcome resistance was applied then the dial
cord slipped off the small drum on which it's wound.
Once the assembly had been detached
it was clear that all was not well. Sometime in the dim distant
past a tiny pulley must have come loose and this had been refitted,
not with a simple wire axle but with a steel pin (another term
for a nail). My guess is two things resulted... firstly, superglue
had been used to fix the pin in the plastic moulding and this
had travelled up the pin and seized the pulley and secondly,
the pin had rusted. The result was a completely seized pulley
and this had affected smooth running of the dial pointer. Whether
this alone had messed up the mechanism remains to be seen.
As I haven't come across any
other description of this repair I've provided the following
set of pictures. |
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You can see there are two independent
dial cords. That for the range switch rotates the drum and needs
investigating due to stiff operation whilst the second, for pointer
movement, is in a mess.
Note the cord has slipped
off the RH pulley resulting in extreme slackness in the dial
cord, and it unwinding from the black part as soon as the tuning
gear was moved. |
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The pulley block now detached
from the housing revealing a stain at the RH pulley centre. The
copper grease on the range pulley is from earlier attempts to
free this part of the mechanism.
Note also the slightly odd design
of the black part on which is wound the dial cord. A screw is
provided to fine tune the amount of take-up of the dial cord
at one end of the dial.. a sort of fiddle factor. |
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The metal pulley was tricky
to detach from its metal shaft as any slip might have wrecked
the plastic parts essential for operation. I had to smooth the
shaft with emery paper to refit the pulley.
Below, the tiny seized pulley
removed with its steel pin.
To part the axle from the pulley
wheel (ie. break the superglue bond) I aligned the head of the
pin over the hole in a square dexion style nut and tapped the
end of the axle with a hammer. Fortunately this worked and I
was able to clean up the axle and refit it in the pulley then
the plastic T-piece. No more superglue used.. |
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The next step is to reassemble
the parts on the dial assembly and check for smooth operation
of both the range and the tuning mechanisms before refitting
in the equipment. To align the tuning I guess I'll need to power
the equipment and adjust it without the dial to a specific frequency
then set the dial to match this and refit it.
Reassembly of the dial assembly
was easy enough and after using copper-ease on the plastic range
ident and its ball bearing the switch changed from ropey and
stiff to perfect. The tuning dial was also perfect without any
glitches. Turning to the front panel, before refitting the dial,
I found the cavity tuner was pretty stiff compared with the one
in my 8640B. WD40 on the front bearing and the bearing on the
front of the cavity had no real effect.
There are two potentiometers
driven by plastic gears from the cavity tuner. One of these gears
is cracked but the crack closes up in operation with only a slight
glitch. I might be able to glue this but I also need to fix a
missing tooth on the cavity gearwheel and this would mean detaching
all three gears. This looks tricky without removing the whole
front panel. In fact I just detached the cavity tuner and moved
it back abut an inch. After a lot of experimentation I discovered
the circlip holding the large plastic gea wasn't fitted into
a slot but just gripping the shaft so I was able to lever it
off, removed the large gear and then the two smaller gears after
slackening their pairs of 0.05 inch hex screws. |
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The worst gear has a split
between a pair of teeth so I pressed out the brass bush and turned
this down so it would slide back into place after gluing the
cracks. This was only partly successful because the crack opened
slightly but I can refit this gear to its pot in such a way as
to avoid the slightly wider spacing beteen two of the teeth.
This is because the pot does not turn a full 360 degrees.
The second smaller gear had
numerous cracks but not extending to the teeth so I glued a metal
washer on the bush to revent further damage. I also fitted a
similar washer to the first gear.
The most difficult task will
be to fit a new tooth to the larger gear as this missing a tooth.
I reckon I might be able to repair this by gluing a sliver of
plastic in its place. The new tooth will measure 6.5mm x 1.5mm
x 1.1mm thick and will need to be profiled to match the mating
gearwheel teeth. |
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A sliver of plastic glued
in place. I found a flexible plant marker which was 1.1mm thick
and cut a tiny section using a scalpel to match the teeth but
allowing some excess so that the material could be scraped to
match the other teeth. The key check was using a vernier caliper
to measure the diameter across opposite teeth. Once this was
within 0.1mm by scraping and filing, I contoured the edges of
the plastic with the scalpel until it roughly matched the mating
gearwheel without dragging. |
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During the above repair,
whilst the glue was curing, I checked to see if other options
were possible and found that one could add baking powder to superglue
to fashion a hard material which could be roughly contoured using
the mating gear whilst still flexible. A third option is to use
something like a JB two-part epoxy and a miniature hand tool
fitted with a tiny cutting disc and a dentist-style drill.
Refitting the set of three gears
proved the repairs were successful. One pot goes from near fully
clockwise to near fully anti-clockwise whilst the other is opposite
going from anti-clock to clockwise. I'm not sure whether the
position of the two pots is critical but if it is I can reposition
the relevant gear on the pot.
Maybe new gears are available?
I counted 80 outer teeth and 12 inner teeth, but the diameter
is critical because the outer teeth mate with a steel gear on
the cavity tuner and the inner drives the twin pot gears. Maybe
an interesting option is to use a 3D printer?
Anyway.. moving on to the next
issue. Revisiting the display.. below is the space where it fits. |
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I fitted the display box
back in place after sorting out a seized pulley and rethreading
the cord. Tuning worked almost to the RH end where the pointer
jammed followed by a loud click from the display box. Tuning
backwards revealed something had gone wrong so off with the box
and a second investigation began. After several failures I put
a 6 inch ruler against the inner edge of the front panel and
found it was slightly bowed.. maybe by only 1 to 2mm but that
together with corrosion was causing the pointer to jam. I scraped
and filed away corrosion and tried again. This time it was better
but the pointer still jammed. I found the outer surface of the
pointer had a lump of dried glue sticking out so I filed this
off. Of course we're dealing here with maybe 0.1mm or so and
the front panel bowing is at least 1mm at the point of jamming,
but finally the pointer moved freely.
At this point I needed to fix
the range display. I'd already applied grease to the mechanical
bits and this allowed the range mechanism to switch.. albeit
with some resistance. My 8640B was much the same and to reduce
the resistance I'd modified a metal indent in the filter box
but this time I didn't bother to do this.
One practical problem is fitting
a range switch knob. Because of its years of use, ending in a
(major?) problem the original range switch knob was now merely
a brass bush which I'd removed. Looking in my junk box I found
a suitable knob but it slipped on the shaft, so I had two options..
file a flat on the quarter inch shaft or find a decent knob.
The diameter was key because the range marking scale needed to
be visible or I'd have to make a paper copy of larger diameter.
Fortunately a third rummage revealed a correct sized knob having
large Allen screws so I glued the scale to this and put it in
place as you can see below. |
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The original range knob
has a lever (much like that on the left) which gives a decent
mechanical advantage to overcome switch stiffness. |
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The display box range
switch worked fine on the bench but once refitted into place
it just jammed solid and the dial cord flew off one of the pulleys.
Already fed up with getting
the tuning dial sorted there was no option but to virtually repeat
the whole process to fix the range drum mechanism (without upsetting
the working tuning dial!!)
On the bench everything worked
smoothly.... the green plastic gearwheel rotated and flipped
the drum to all its settings without a hitch but as soon as the
box was fitted and the four fixing screws were tightened the
thing jammed solid.
On the right is the left end
underside of the display box with the two outer holes for very
long securing screws and that centre hole.. for what? |
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Well, the end of the range
drum locates over a plastic end cap with a tiny pip to ensure
correct positioning. The drum has a pulley around which is fed
dial cord and the pulley connects to an ident switch whose position
is fixed by a ball bearing held by a strong spring. The end cap
is therefore under some considerable stress and to fix it in
place there are several screws. Two of these screws locate the
end cap securely in position whilst the two long screws holding
the box to the chassis also have a measure of control over the
end cap position. I found the problem resulting in jamming was
the end cap was being skewed by the box fixing screws because
that centre screw was loose. Using a light and magnifier I found
the plastic into which the fixing screw threads had a piece missing.
After puzzling over this I realised that someone had fitted an
oversize screw and broken the plastic. The end cap wasn't held
in place properly and the drum was jamming. Can I drill a couple
of small holes either side and use new screws to do the job?
In fact this wasn't necessary because I found the real problem
(or had I?). |
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I began to remove screws
from the complete but totally seized display assembly. Starting
with removing the ident spring just in case for some odd reason
the ball and spring were seized.. but they weren't and detaching
the spring had no effect. To give you some idea of the problem,
attempting to rotate the end pulley or the eighth inch axle at
the other end (above right) proved impossible. Even rotating
the drum itself was impossible so could the axle bearing or the
bearing at the rear of the pulley be seized?
I removed the front bezel and
then the two countersunk screws holding the black metal extrusion
to the end plates and suddenly the drum freed up completely.
What's happening is akin to operating a drum brake in a car.
Above right you can see a gap between the end plate and the extrusion.
If the gap is present... no problem, but closing the gap locks
the drum. Basically any screw that closes the gap locks the drum
in place and this includes the pair of very long screws holding
the display box to the chassis. A straight edge along the drum
confirms that it's not distorted, neither is the black metal
extrusion. |
I looked at the driven
end of the drum to see if that had the same problem but it didn't.
The end plate was snug against the extrusion and the drum didn't
bind. Note that the spring between those two upper lugs has been
temporarily detached to permit freer drum movement during testing.
You can see everything is not
perfect here as the plastic pulley has cracked. Without removing
the cord I can't superglue the crack so it's a problem for the
future. Copper grease has been used on the detent mechanism.
The fix for the jamming needs
to be thought out. First I'll check no parts are distorted, and
if everything is OK I think I'll put down the problem to plastic
shrinkage or maybe more likely, slight distortion in the drum.
The fix might be to add shims to prevent the gap between the
end plate and the extrusion from closing up. |
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This picture shows the
underside of the display box. When the drum is free to rotate
the extrusion is proud of the underside of the end plate by 1.56mm
or a sixteenth of an inch. That means I need to add a sixteenth
of an inch shim under the end plate to prevent the gap closing
and the drum to lock up.
Because of the way the gear
wheels driving the range drum and the tuning pointer mesh with
mating gears under the chassis, the effect of this shim needs
to be tested otherwise an alternative solution needs to be found.
However, as the underside of the extrusion will still be flat
against the chassis I think the shim under the end plate should
be fine. |
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I started to test the
hypothesis by first of all checking to see if there was a way
to easily fit the new shim and found that by making it about
3 and a half inches long and 11mm wide (don't say anything) a
shim would bolt into place at the extreme edge of the chassis.
I removed various screws in the display box and refitted them
to check no other problems existed and the fault was repeatable.
At about the same time I'd discovered
that, with everything in place, the extrusion was no longer proud
of the endplate, AND with the drum rotating freely, and wondering
why this was so... something fell to the floor. I picked it up
and saw it was a small piece of black plastic with part of a
thread visible. Without pondering this I looked at the end plate
and found no gap... I also noticed the end of the axle was dead
centre in its hole and the drum turned perfectly freely... then
the penny dropped. The piece of broken plastic had been jammed
behind the drum and sure enough when I looked at the drum closely
there were now slight score marks visible where the plastic bit
had squeezed out when I was jiggling the drum to check for clearances.
Below.. you can guess where the plastic part had been stuck.
Behind, where the gap was widest, between the black metal extrusion
and the back of the drum. |
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After umpteen attempts
the end plate suddenly fitted perfectly. After and before >>> |
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Here's the tiny piece
of plastic that gave all the trouble. It was probably responsible,
not only for the drum jamming but also for the pointer sticking
because the clearance between the drum and bezel at the RH end
was lessened. No doubt the seller or the previous owner had broken
the range knob, broken a tooth off the tuning pulley and these
faults had ended the life of the 8640A.. at least temporarily
as it was probably working electrically at the time.
The thread gave up when an oversize
US screw had been forced into it. |
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I need to refit the display
box to the chassis.. check everything works properly mechanically,
then plug it in and see what happens. This went fine with both
tuning and range working smoothly. |
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Initially the RF meter
read close to zero but the three meter select buttons weren't
latching. I poked at these a few times and the RF meter suddenly
came to life with 0dBm indicated. This was maintained as the
range switch was moved to different frequency bands.
I used my Tiny SA (spectrum
analyser signal generator) to confirm everything was OK.. as
above for 100MHz and below at 200MHz and 800MHz (this example
includes the 500-1000MHz range). |
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I now need to use a spot
of switch cleaner to free up the meter switches and the modulation
switches etc. then finish the cosmetic work, mainly filing the
scabby aluminium to make it look half presentable. Then check
everything works as per spec...
It's unfortunate that aluminium
alloy corrodes over time when in damp conditions. Salt present
in the water makes things very much worse and I remember way
back in the late 1960s seeing this for the first time. Our
factory in Liverpool made computers. This was donkeys years
before tiny PCs, in the days a computer was pretty big. Ours
were around seven feet high and built in stove enamelled cabinets
with plenty of chrome bits and pieces. A typical computer had
maybe five or more cabinets and in terms of real time operation
were actually quite powerful. Our boss decided he'd sell some
of our computers to Russia. I'm pretty sure he wouldn't have
been allowed to actually follow through because of the cold war,
but nevertheless he arranged for a computer to be shipped to
a Moscow trade fair. Because computers were notoriously tricky
to get working lots of test equipment went with it. I guess things
went tolerably well but alas the stuff was shipped back to Liverpool
on the deck of a boat and the Tektronix and HP oscilloscopes
were ruined. We never did sell a computer to Russia but we did
sell an air defence system to Burma using those very same XL9
computers. |
Initially I found the
output RF indication on the meter was intermittent and sometimes
zero so detached the pair of circuit boards adjacent to the meter
and freed up the set of three push-button switches which were
reluctant to lock into position, but replacing them still hadn't
fixed the intermittency. I soon found this was associated with
the attenuator rotary switch, most likely the rear-mounted parts.
After rotating a few times and with the application of switch
cleaner the intermitency was resolved.
The next task was to confirm
the tuning dial corresponded to the RF output frequency. The
dial read something like 101MHz at 100MHz output so I tuned the
output to precisely 100MHz then loosened the two screws at the
end of the dial box. After clearing the metal gears from meshing
(cavity tuner and dial box) I turned the dial to 100MHz and refitted
the two screws. The dial now reads the output frequency. The
design doesn't include anti-backlash gears and, because the cavity
tuner is deliberately made stiff (which I understand is to make
it stable), tuning to zero beat on a test receiver is a bit messy,
but drift is negligible and mechanical stability excellent. All
the testing in this these tasks was completed using an SDR Play
which tunes from a few KHz to several GHz.
I also tested the RF output
level and the SDR dBm readings followed the settings on the attenuator.
At higher output levels I needed to add a couple of in-line attenuators
20dB and 10dB to overcome receiver saturation. During tuning
and modulation tests I used AM as this gave an easier way to
check tuning. Switching to FM gave rather strange results so
I need to look at the user manual and perhaps track down any
faults. For example, when I set the FM dial to say 20KHz deviation
the signal on the test receiver jumped from say 100MHz to 100.02MHz.
In the 8640 FM is achieved in rather an odd way and I suspect
there's a faulty component lurking.
A couple of annoying things
showed up. One was modulation knobs binding and the other was
the attenuator dial was offset and not all the marked settings
were possible. The latter might be to do with linkages not aligned
with the main attenuator switch or even the wrong dial fitted
to the atteuator. Again a study of the user manual will help.
During testing the rear-mounted
fan was very noisy so I squirted it with switch cleaner and after
an hour it ran silently. I checked a random electrolytic capacitor
to see if there's any clue to these failing but it read the exact
capacitance with a very low ESR so hopefully none will need swapping. |
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Reading the manual I noted
the power supply rail voltages and their test points and adjusters
so I initially removed the boards as you can see above. All the
rails use two capacitors, one for smoothing and a second in the
control circuit. I checked all of these and found every one was
in a very poor state so removed them and fitted new.
Upper left supplies neg 5.2
volts, upper right plus 5.2V and plus 44.6V. Left supplies neg
20V and plus 20V. |
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Capacitance/Rating |
Capacitance/ESR |
Replaced with |
33uF x 10V |
37uF x >40 ohms |
47uF x 16V |
33uF x 10V |
33uF x 20 ohms |
47uF x 16V |
33uF x 10V |
33uF x >40 ohms |
47uF x 16V |
33uF x 10V |
33uF x >40 ohms |
47uF x 16V |
33uF x 10V |
33uF x >40 ohms |
47uF x 16V |
33uF x 75V |
33uF x >40 ohms |
47uF x 63V |
220uF x 9V |
208uF x >40 ohms |
220uF x 25V |
300uF x 10V |
104uF x >40 ohms |
470uF x 50V |
300uF x 25V |
62uF x 21 ohms |
470uF x 50V |
300uF x 25V |
61uF x >40 ohms |
470uF x 50V |
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As you can see all the
old capacitors have very large ESR values although oddly some
have maintained their marked capacity.
As an example the larger values
should have an ESR of less than one ohm whilst the smaller something
like up to 5 or 6 ohms. |
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Power supply capacitors
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During testing I'd noticed
the fan was intermittent and soon it needed a little push to
get it going but, after replacing the capacitors in the three
power supply boards, nothing would persuade the thing to run.
I imagined it was in need of lubrication because earlier on it
would make a rough start. Getting it out of the chassis looks
tricky but I worked out it could be done fairly easily. The horizontal
mounting bracket is in two halves held together by two small
screws. The bracket is also screwed to the rear metal casting
and these two screws can be removed using a short pozidrive tool.
Then the two screws holding the horizontal bracket are removed.
Note that these are non-magnetic stainless steel so don't drop
them into the chassis. once the top bracket is detached the fan
body can be slid backwards so the fan blade is clear of the rear
casting, and the electrical connector just lifts off the regulator
board.
The blade is held in place by
a grubscrew which can be slackened with a 5/64th Allen key (no
other size should be used). The key may need jiggling if oxide
is present. To remove the blade you might need to lever it off
using pliers to grip the shaft for fear of damaging the bearing.
Once off you can lubricate the shaft. The other end of the shaft
is located by a small screw which can be removed for lubricating
this end of the shaft. |
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While the fan is detached
you can clean and then align the blades by rotating it against
a table edge to check each blade position.
Why HP use such a complicated
fan circuit puzzles me but perhaps I can be enlightened?
After lubricating the fan, but
before refitting it, I checked to see if it was OK. Unfortunately
not one jot of improvement so either the thing is kaput or there's
a drive circuit issue.
The user manual suggests testing
the various transistors etc. |
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The fan circuitry is obviously
on the board into which it's plugged so I pulled this out and
checked the two rows of TO39 and TO18 transistors.
I immediately found Q9 had a
short circuit base-collector junction and Q12 was open circuit
base-emitter plus base-collector.
Removing the Q9 proved it was
faulty. The HP code marking is an 1853-050 made by Motorola (the
manual has 1853-007 listed as 2N2351). I fitted a BC261B because
this was my nearest equivalent.
I unsoldered Q12 and found only
one leg remained. As you can see below two legs have rotted through.
I jiggled the adjacent transistors and sure enough Q10 suddenly
had an open circuit base-emitter, so I fitted a pair of 2N4036
transistors in their place. The HP transistor is an 1853-027
(a custom device made by Fairchild). |
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Plugging back the board
and re-installing the fan proved it was now working perfectly.
I have come across this type
of transistor leg corrosion a few times before, but why the TO18
device shorted is puzzling. |
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Now the original fan is
refitted and working I've found it's unduly noisy. The complexity
of the fan circuit (not to mention it's unreliability) makes
me think that back in 1970 or 1971 a group of Hewlett Packard
guys were looking for something interesting to do rather than
come up with something simple and just as effective. Read
this and see what you think.
Fan circuit is below... |
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Anyway I'm considering just removing
it and fitting an ex-PC cooling fan. Of course, as these are
usually 12 volt I'll need to check available supply voltages
and see how it performs perhaps using reduced voltage. |
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